Case Study

Restoring production with HPHT

Restoring production with HPHT

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Serving Every Well Challenge The well was completed as an Open Hole Gravel Pack with 5 ½” screens in a 9.5” OH. The initial gas production was over 200 MMSCFD, however due to the well liquid loading, after 3 years the production went to zero, resulting in the well being shut-in for 2 years. Interwell’s objective was to achieve water shut-off or water slow-down so that production could be re-established. Region/Field: Key Capabilities: • Pat

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