Case Study

Octopus slimhole ESP packer saved $800,000 USD in workover costs

Octopus slimhole ESP packer saved $800,000 USD in workover costs

Pages 2 Pages

Octopus slimhole ESP packer saved $800,000 USD in workover costs Challenges • Aging offshore well with casing integrity issues • Well required ESP to produce economically • ESP was installed in a deviated section of the slim, 5 in.-ID production liner • Cost-prohibitive casing remediation and recompletion options • Hang-up risks associated with deploying an eccentric feedthrough ESP packer Results • Re-established well integrity by isolating the damaged casing • Enabled continued, economic production from aging well • Reduced ESP workover costs by an estimated 50% • Increased packer deployment reliability via a concentric through-bore design • Executed flawless installation of the industry’s first 5-in. concentric ESP packer A customer in th

Join for free to read