Case Study

Increased Run Time More than 720% with SXD ESP Pump and Diverter Valve

Increased Run Time More than 720% with SXD ESP Pump and Diverter Valve

Pages 1 Pages

Case History Mississippi Chat operator had a well with excessive shutdowns. These shutdowns were often a result of excessive gas. The operator had issues producing gas up to 3 Mcf/D through the electrical submersible pumping (ESP) system and this problem caused the variable speed drive (VSD) to go into underload multiple times per day. During shutdown, solids and sand lodged in the pump. When the operator attempted to restart the system

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