Case Study

Using Dirty Service Trim in Critical Valves Provides Four More Days of Uptime per Year

Using Dirty Service Trim in Critical Valves Provides Four More Days of Uptime per Year

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D352707X012/Sept17 For more information: www.Fisher.com POWER Using Dirty Service Trim in Critical Valves Provides Four More Days of Uptime per Year RESULTS • Eliminated the build-up of magnetite and plugging of the valve’s cage and seat • Avoided shutting down an HRSG unit to acid-clean the valves, saving $30,000 USD and two days of lost generation per unit, per procedure • Extended runtime in a critical-to-process application APPLICATION Drum level control valves in triple-pressure, feedwater service CUSTOMER Combined-cycle plant in central Florida, USA CHALLENGE A combined-cycle plant operates with multiple power blocks. Each block has two combustion turbines and two triple-pressure heat recovery steam generators (HRSG) that feed into a common steam turbine. The three pressu

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