Case Study
Industrial Warehouse - Nashville, Tennessee
his 300 ft by 900 ft single story, slab-on-grade structure was built in 1971. Over time, the western portion of the building had settled up to 15 inches. This caused the heavy, pre-cast concrete wall panels to skew and tilt out of plumb up to 8 inches over their 30-ft height, stressing the roof system. The geotechnical evaluation showed a surficial layer of dense gravel extending a minimum of three feet below foot- ing level. Beneath this was a