Case Study

AGR plans and drills a vertical exploration well during multi client campaign in Browse Basin

AGR plans and drills a vertical exploration well during multi client campaign in Browse Basin

Pages 2 Pages

The complicating factors: • The tidal currents in this region were much stronger than expected based on available information which affected operational performance • Failure of port crane engine delayed the start of the campaign and resulted in 25.25 hrs of down time while it was assessed and repaired • A Maritime union strike affected the availability of 3 out of 4 anchor handling vessels for a 24hr period during the campaign APPROACH

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